Update 10-28-09: Finally!
After what was the most painful mid season that we have ever experienced, man did things make a great turn around for us. We just finished the biggest race of our short racing career at the ORTC Boost Vs. No Boost Race in Bradenton Florida. We arrived about mid afternoon last Thursday. Wanting to put as few passes on the brand new motor as possible, we arrived to find out that we had to get our NHRA license. So right off the rip, there went plan number one. We unloaded and proceeded to prep the car for what was going to be a long weekend. After getting the ole heap hot and bothered, down to the line we went like little school kids. Once near the line, I reached up and hit the loud button. Dang what a sound this thing has now. It means business. I burned in, did the staging routine, lit the ambers, and was off like a....snail. A really bad spinning snail! In other words, we missed the tune up for the new radials. After a brief cool down, laugh, and changes, back to the line we went. This time after the aforementioned procedure, when I let her go, she pinned my head into the seat like a school yard bully, pulled the front tires when the 2nd system turned on, and proceded to fly to half track where I clicked her off for a plug read. We coasted a 5.12 @ 115. Thats just sick for how our year has gone! We came back made some changes, and decided we would find the back door this time. Once again, lite up, burn in, etc, etc. This time, when the front tires lifted, they stuck there only to touch down right before half track, and dump out a 4.84 @ 148! For the air conditions, the weight, and pill set, we were more than pumped! Friday brought us more testing, and the first round of qualifying which netted us number 2 out of about 30 cars with a 4.94 @ 148. This was mildly promising, but we needed more. A lot more. Saturday brought us two more rounds of qualifying where we ended up number 2 for good with a 4.90 @ 148. This was ok, but I was struggling bad with the tune up. This car had so much more in it that it was silly, but I could not find it for the world! Sunday morning, the ole heap and I had a talk. I explained that I really didn't want to go home until Monday so there was no need to rush gettin back in the trailer. Got my point? First round bye run in the heat we ran a 4.90 again. This was really good as the heat had been slowing us down tremendously! Second round, we snuck by our competition with a 4.89 @149. Notice the MPH? We were working on something. Next round, we got a little greedy on the tune up. This is where the drama begins. When I let the ole girl breathe, the took a real deep breath and we started into a wheelie from you know where. Much to my surprise, I pumped the gas one time and down she came smooth as silk. Only to reward me with a 4.98 @ 151. Notice the MPH?? We were dead on this thing now. Semi finals of No Boost class, saw us lay out a 4.87 @150.95, and a spot into the FINALS of the biggest race of the year! We lost in that round to a killer pass by Jason Black, but we found something in the car that we didn't even know existed. With a 1.26 60', we went a 4.82 @ 151! We were pumped and heading into the semi's of the Boost Vs No Boost Challenge. We had to race Mustang Mike with his twin Procharged Monster. When he and I bumped the ladies in, imagine my surprise to ride a wheelie out, pump the gas, and still win the round. What? That was not supposed to happen. REALLY glad it did, but it wasn't supposed to. Here we go into the finals against the Procharged Monster of Tony Ridnour (spelling??). By this time, the weekend was already a dream come true, and we were pumped to the moon. But, I found something in the tune up again. With a slight adjustment to what should cause the 60' to get better, and leaving the previous 4.82 tune up in otherwise, we were on a mission to set a record. When we loaded the ole girl into the beams, hopes were high, but trouble was looming. We drilled the tree, cut a 1.20 60', and were decently out on the Procharged monster to our left when suddenly, she nosed over. What?! Making a very long story short, a syphon tube broke off our number 1 systems' bottle. We ran a 4.98 @ 143 on 1 kit! But we lost. No hard feelings though. After the year we have had, to go and do this well is simply a dream come true. I couldn't have done it without my Team. Chad and Randy were priceless this weekend. Thanks again to all our sponsors on the front page as well. If you are buying something that these people make, and you buy another brand, it will be the first of many regrets for you. These people stand behind racers, care about them, and do what it takes to keep you moving. Thanks again to everyone. We have some big decisions, and major changes happening right now. Keep tuned. You won't believe this!